Bubble
1. Justification and discussion
of the process optimization and possible mold redesign. Include what problems occurred if any and give
reasoning behind the parameter adjustments or mold modifications that were made that improved the
condition.
The thermoform component in our yoyo is the clear bubble. We had no
major mold redesigns. In fact, we kept the dimensions fixed and redesigned the
inner diameter of the inner ring to fit closer to the outside of the bubble. However
during the first runs, we ran into issues with the plastic not being fully
flush around the pegs due. This posed a problem in the long run because the not
flush plastic would cause a weaker seal
between the housing and the flat of the bubble thermoformed part,
increasing the likelihood of water seeping out. The problem was primarily
because there were not enough air holes around the die-cut pegs to allow the
hot plastic to nicely conform around the pegs. We started with stainless steel
pegs and then tried coiled pegs in hopes of making use of the interface for air
to pass through and suck the plastic. The coiled pegs did not provide enough of
a gap and we resorted to filing a flat in brass pegs and filing into in the peg
holes in the mold. These corrections significantly improved the thermoformed
part. We also changed the thermoform parameters to make the plastic conform to
the pegs further. Below is table of our tested parameters for various runs.
Run 1
|
Run 2
|
Run 3
|
Run 4
|
|
#02 Heat Time
|
150
|
225
|
225
|
225
|
#03 Form Time
|
100
|
100
|
200
|
175
|
#05 1st Platen Open
Delay
|
150
|
150
|
200
|
200
|
#06 Cooling Fan Delay
|
25
|
25
|
25
|
25
|
#07 Cooling Fan Time
|
100
|
100
|
100
|
150
|
#08 Air Eject/Platen Hold Time
|
5
|
5
|
5
|
5
|
#12 Main Vacuum Delay
|
3/0
|
3/0
|
3/0
|
3/0
|
#13 Main Vacuum Time
|
100/0
|
100/0
|
100/0
|
100/0
|
Top Oven Temp
|
650
|
675
|
650
|
650
|
Bottom Oven Temp
|
650
|
675
|
650
|
650
|
Figure 1
Figure 1 shows the results from the 4 runs. At first, we increased the
heat time and oven temperature so that the plastic would be more amorphous and conform
to the pegs. Run 2, however, was too hot and did not hold its shape during
demolding. To correct for this, we brought the temperature back to 650 and
maintained the heat time while adding longer form time to allow the part to
cool longer. We also increased the open delay a bit. Run 3 was pretty
successful but we wanted to corrected one more time to get the plastic to
conform to the pegs even better. The plastic was still pretty hot so we
increased the fan cooling time. We decreased the form time slightly to activate
air eject, which would break the vacuum and assist the formed part off the
mold. Run 4 was successful. Each run is about 40 seconds.
However, after 20 runs, we realized the thermoformed parts were
decreasing in quality. Figure 2 shows the results after 20 runs. Some parts
were coming out not holding shape due to the machine overheating and some parts
were not fully conformed to the pegs. We supposed this issue has to do with the
faulty air compressor. For this lab we made 30 successful parts using the 2.999
diameter circular die-cutter.
Figure 2
2. A fully dimensioned drawing of the part. In the event of a redesign,
a fully dimensioned revised
drawing showing the new design specification as well as a fully
dimensioned revised drawing of the
mold including matching revision levels.
4. Update the posted Gantt chart. (Your team’s component(s) only).
Due to the faulty air compressor, we will need to wait and hear back
from the 2.008 staff to complete another production run. Alternatively we can
produce 20-25 parts in a batch and wait 10 minutes before starting another
batch. The thermoformed bubble part will be completed and die cute by the end
of next week.
5. Post your component’s set-up
sheet showing all the optimized parameter settings that will be used to run production for the component.
#02 Heat Time: 225
#03 Form Time: 175
#05 1st Platen Open Delay: 200
#06 Cooling Fan Delay: 25
#07 Cooling Fan Time: 150
#08 Air Eject/Platen Hold Time: 5
#12 Main Vacuum Delay: 3/0
#13 Main Vacuum Time: 100/0
Top Oven Temp: 650
Bottom Oven Temp: 650
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